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![]() 568 Posts Member #: 1200 Post Whore Bristol |
24th May, 2009 at 10:19:41pm
Hope someone on here can give me a pointer in the right direction!
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559 Posts Member #: 2775 Post Whore Aberdeen |
24th May, 2009 at 10:25:07pm
Do the obvious like you have said and do a compression test. The results of that will point you in the direction of what to do next. But past experience would say it is going to be pull the cylinder head. It sounds like the head gasket has gone. What spec engine are you running? |
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![]() 568 Posts Member #: 1200 Post Whore Bristol |
24th May, 2009 at 10:35:15pm
its a N/A 1293 with a stage 3/4 head and some nice internals and full roller rockers.
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![]() 8297 Posts Member #: 408 Turbo Love Palace Fool Aylesbury |
24th May, 2009 at 11:42:05pm
Sounds like head gasket if the water system is being pressurised. https://www.facebook.com/pages/Fusion-Fabri..._homepage_panel
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![]() 1346 Posts Member #: 2340 Post Whore Dublin Ireland |
25th May, 2009 at 08:44:43am
Don't wip anything off untill you have done a compression test and reset the tapit clearence and changed. When you do the compression thest watch the guage the first kick is most umportant make sure your trottle is full open and all other plugs out. On 17th Feb, 2009 Rob H said:
I find the easiest way is to super glue the bolt to the end of one of my fingers. ______________________________________________________ |
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50 Posts Member #: 5265 Advanced Member telford |
25th May, 2009 at 09:19:04am
i had a prob like that no oil water mix but head gasket broke between 2 and 3 cylinders garlic bread |
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![]() 568 Posts Member #: 1200 Post Whore Bristol |
25th May, 2009 at 07:12:33pm
cheers lads, I realised this morning i dont have a compression tester in the tool box, so off to helfrauds tomorrow for one! after speaking to a couple of other people they have suggested i may have blown it between 2 and 3! will let you know the results soon.
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1394 Posts Member #: 1346 Post Whore bromsgrove |
25th May, 2009 at 07:47:35pm
IMO, before whipping anything off, give it a service, plugs, leads, points and condensor. coil.
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![]() 568 Posts Member #: 1200 Post Whore Bristol |
25th May, 2009 at 09:10:41pm
It had a new coil and condensor a couple of weeks back, for some reason the dizzy seems to eat them, so thats getting changed tomorrow! will then check the compression and the valve clearences! and then if all else fails whip the head off time! |
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![]() 9812 Posts Member #: 332 Resident Cylinder Head Modifier Mitsi Evo 7, 911, Cossie. & all the chavs ...... won no problem |
26th May, 2009 at 05:25:35pm
my guess is the the head gaskets gone between 2 and 3 bore
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![]() 568 Posts Member #: 1200 Post Whore Bristol |
26th May, 2009 at 09:21:39pm
update time, whipped the head off and everything looks ok, the gasket is in one piece with only a bit of discoluration between 2 and 3! the only thing that seems out of place is the colour of the inlet on number 3 cylinder! looks as though it may be that thats stuck?, that would explain the fuel being pressurised out of the carb and the engine not running! will take it apart tomorrow and see if anythings amiss, any pointers greatly appreciated!
Edited by pickmeup on 26th May, 2009. |
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869 Posts Member #: 2443 Post Whore Cheshire |
26th May, 2009 at 09:33:51pm
I aggre that something undue has/is occuring in cylinder 2. What are the pistons and bores like. Was the manifold gasket in one piece? Have you checked the rockers and pushrods for fatigue, failure and bending? Intresting one this. |
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![]() 568 Posts Member #: 1200 Post Whore Bristol |
26th May, 2009 at 10:54:14pm
the pistons and bores are fine, doesnt seem to be any real play in the rockers either? will strip and rebuild the head and then slap it back together, nothing much else i can do? |
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![]() 3329 Posts Member #: 184 Senior Member Melton Mowbray, Pie Country |
27th May, 2009 at 08:16:01am
What did the compression test show? http://www.twin-turbo.co.uk
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559 Posts Member #: 2775 Post Whore Aberdeen |
27th May, 2009 at 09:39:41am
On 27th May, 2009 Ben H said:
What did the compression test show? |
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530 Posts Member #: 1192 Post Whore In the garage......again!! |
27th May, 2009 at 09:38:38pm
On 27th May, 2009 Ben H said:
What did the compression test show? My guess is you tore it down without a comp test eh?:) 133.5 bhp 123 lb torque 116mph @6640rpm 9.5psi
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![]() 568 Posts Member #: 1200 Post Whore Bristol |
27th May, 2009 at 11:09:00pm
the compression test showed no probs! was 120 on all cylinders which i thought was strange! Ive got the suspect valve out now and it seems ok, gonna check it at work in the metrology dept then re-lap and stick it back in, really confused by it as nothing seems that wrong! |
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2497 Posts Member #: 1954 Post Whore Luton Bedfordshire |
28th May, 2009 at 01:49:21pm
Sounds like the head gasket has failed. By that I mean seperated between the layers and split one of the combustion rings. Number 2 looks like its had some water in there and the presurised water system fits the pattern. very hard to spot and wont show up on a compression test. Had this happen to me a couple of times, over tightening the head bolts is the main cause. Own the day
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![]() 568 Posts Member #: 1200 Post Whore Bristol |
28th May, 2009 at 10:24:44pm
i will have a good look at the head gasket tomorrow and see if i can see any witness marks of it! ive had the valve measured and its only 0.02mm out between max and min and its straight so no probs there! Ive re-lapped and installed the valve and may stick it all back together tomorrow, I had planned on fitting my weber box too while theres room but will probably leave that for the time being!
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![]() 568 Posts Member #: 1200 Post Whore Bristol |
30th May, 2009 at 08:02:16pm
Checked over the valve lift and tdc on the engine and all seems ok, silly question though should the dizzy at TDC on no1 cylinder point to the cylinder as its pointing at 4o'clock, but its been running like that for 3 or so years!
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2497 Posts Member #: 1954 Post Whore Luton Bedfordshire |
1st Jun, 2009 at 12:36:37am
No. It all depends on how the dizzy shaft was positioned when the dizzy was fitted back into the block. So long as you know where the rotor arm is pointing at TDC you can workout which lead goes where. Own the day
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![]() 568 Posts Member #: 1200 Post Whore Bristol |
12th Jun, 2009 at 10:16:10pm
quick update
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3006 Posts Member #: 2500 Post Whore Buckinghamshire |
12th Jun, 2009 at 10:54:56pm
More haste, less speed !! |
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![]() 568 Posts Member #: 1200 Post Whore Bristol |
12th Jun, 2009 at 11:01:59pm
yep i know |
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![]() 1497 Posts Member #: 100 Parisien Turbo Expert Paris\' suburb |
13th Jun, 2009 at 09:26:05am
secound that you head gaskt has gone, and it can't be seen on comp test , have have this previously on many minis, looking at your secound pic showing the head and gskt in place, on the left the fire ring around the bore is burned.
On 28th May, 2009 Mr Joshua said:
Sounds like the head gasket has failed. By that I mean seperated between the layers and split one of the combustion rings. Number 2 looks like its had some water in there and the presurised water system fits the pattern. very hard to spot and wont show up on a compression test. Had this happen to me a couple of times, over tightening the head bolts is the main cause. Edited by fab on 13th Jun, 2009. |
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