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| Home > Help Needed / General Tech Chat > Turbo Minivan - weird misfire from cold on cylinders 1 & 2. | |||||||
![]() 1105 Posts Member #: 1504 Post Whore Westbury, Wiltshire |
30th Jan, 2011 at 10:08:40pm
Hi guys.
Minivanless, but reluctantly happy living with the decision. There'll be another one day.
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![]() 12307 Posts Member #: 565 Carlos Fandango Burnham-on-Crouch, Essex |
30th Jan, 2011 at 10:17:22pm
hummm, weird,
On 28th Aug, 2011 Kean said:
At the risk of being sigged... Joe, do you have a photo of your tool? http://www.turbominis.co.uk/forums/index.p...9064&lastpost=1 https://joe1977.imgbb.com/ |
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![]() 1105 Posts Member #: 1504 Post Whore Westbury, Wiltshire |
30th Jan, 2011 at 10:48:46pm
On 30th Jan, 2011 Joe C said:
hummm, weird, try swapping the plugs round? 1&2 with 3&4? shut the plug gaps up a bit? Yep Joe. Tried swapping plugs 1&2 with the 'good ones' 3&4 but the problem still comes back to plugs/cylinders 1 & 2. Tried closing the gap down to 0.022 but no effect, so took them back to 0.028. Anyway, this is the gap I've always used and with the stronger spark from the coilpack, I'd argue this should be more like 0.032. 0.028 is a good compromise at the mo for testing til I get the misfire sorted. I just wished I could chuck a dizzy in but I sold mine at the end of last year - dohhhh, what a muppet !!! Anybody local got a dizzy and coil I could borrow ? Richard. Edited by turbominivanman on 30th Jan, 2011. Minivanless, but reluctantly happy living with the decision. There'll be another one day.
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5988 Posts Member #: 2024 Formally Retired Rural Suffolk |
30th Jan, 2011 at 10:57:57pm
On 30th Jan, 2011 turbominivanman said:
Could it be something to do with the dwell and spark durations in Megasquirt as I’m sure Rod S posted something up a few years back about the Ford coilpack being sensitive when directly driven by igniters in the ECU ? It was Paul S rather than me who pointed it out but yes, the coilpack is sensitive to charge/dwell times with Megasquirt when you fire it direct from the MS rather than through EDIS. BUT, as you rightly say, if the charge/dwell times were wrong, or the coilpack degrading because they are wrong, it should affect 1+4 or 2+3, not your combination of 1+2. However, there are some unsubstantiated stories going around occassionaly that Ford did have problems in the early days with wasted spark coilpacks because of the way they work - they don't use ground but as there are actually only two coils in a coilpack, the spark goes from one coil into 1, through 4 then back to the other end of that coil. Likewise, from the other coil into 2, through 3 then back to the other end of that coil. As a result, 1 and 2 get a positive jump, 3 and 4 get a negative jump (if that makes sense). Apparently on some models Ford actually specified a different grade of plug for 1&2 compared to 3&4. Just to rule this out, I would swap the 1&4 leads and the 2&3 leads on the coilpack hence reversing the polarity of the sparks through the plugs but still keeping the wasted sparks on the right plugs. EDIT - note, that is swapping the leads at the coilpack, not swapping the plugs like Joe suggested (end EDIT). Finally, have you done a continuity check, all four HT posts to ground ??? Unlike a normal coil, there should be infinite resistance to ground as the HT should only see ground on its path between the two plugs, not at the coilpack. Rod. Edited by Rod S on 30th Jan, 2011. Schrödinger's cat - so which one am I ??? |
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![]() 4360 Posts Member #: 1459 En-suite user Braintree, Essex |
30th Jan, 2011 at 11:05:00pm
Going off on a tangent....could this be more mechanical issues....sticking valves etc? Got a level compression readings, but was this done warm or cold? Edited by Jason G on 30th Jan, 2011. On 19th Jan, 2010 wil_h said:
I would start the furthest place from the finish. On 24th Mar, 2012 apbellamy said:
I feel all special knowing that I've given your mum my wood. Been neglecting Turbo'd 'A' series.............. |
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![]() 1105 Posts Member #: 1504 Post Whore Westbury, Wiltshire |
30th Jan, 2011 at 11:16:45pm
On 30th Jan, 2011 Rod S said:
..... swap the 1&4 leads and the 2&3 leads on the coilpack hence reversing the polarity of the sparks through the plugs but still keeping the wasted sparks on the right plugs. Yes Rod, have tried the swap at the coilpack as well. No change, regardless of swapping over 1 with 4 or 3 with 2. However, also interesting to note your comments about early coilpacks as the markings on the Ford sticker on the coil for HT posts '1' and '4' on the replacement that came from Almichie (thanks Al), are reversed in my original coilpack. The coilpack has a different part number as well, even though they look exactly the same. On 30th Jan, 2011 Rod S said:
..... have you done a continuity check, all four HT posts to ground ??? No Rod. Good point, I'll do that and report back. Thanks. Richard. Minivanless, but reluctantly happy living with the decision. There'll be another one day.
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![]() 1745 Posts Member #: 375 Post Whore Leicestershire |
30th Jan, 2011 at 11:22:36pm
Can you rev through the miss or is it all the time? Does megasquirt have any trim functions related to coolant temp that could have altered. Seems a strange one. You say the earths are good these gave me some issues with my Megajolt. |
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![]() 1105 Posts Member #: 1504 Post Whore Westbury, Wiltshire |
30th Jan, 2011 at 11:24:34pm
On 30th Jan, 2011 Jason G said:
Going off on a tangent....could this be more mechanical issues....sticking valves etc? Got a level compression readings, but was this done warm or cold? No I dont think this is a sticking valve issue Jason. The comp test was done cold and gave good clean repeatable results on 3 separate occasions. The misfire occurs at cold when you'd expect the vale clearances to be fairly loose as heat hasn't expanded the guides or valves at this point. It also doesn't explain why the strobe flash is slower and with gaps in the pulses on cylinders 1 & 2 - I think this is ignition related IMO, not mechanical. I've also had the rocker cover off to check the tappets and clearances which are all fine and I've spun the engine over and all valves work fine on cranking and when the engine's fired, although I didn't do that for long as the rocker oil goes everywhere ! Richard. Minivanless, but reluctantly happy living with the decision. There'll be another one day.
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5988 Posts Member #: 2024 Formally Retired Rural Suffolk |
30th Jan, 2011 at 11:30:00pm
The only other thing I can think of is your settings in MS aren't ideal for your new lower compression ratio, especially if it only happens when cold.
Schrödinger's cat - so which one am I ??? |
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![]() 1105 Posts Member #: 1504 Post Whore Westbury, Wiltshire |
30th Jan, 2011 at 11:38:40pm
On 30th Jan, 2011 Star Mag said:
Can you rev through the miss or is it all the time? Does megasquirt have any trim functions related to coolant temp that could have altered. Seems a strange one. You say the earths are good these gave me some issues with my Megajolt. Thanks Ron. I would admit, it feels like you can rev through the miss, yes, but if you hold the throttle at say 3k, you can still hear the dull missed beat in the exhaust, so it lulls you into thinking it'll clear. Once back at idle, the miss is audibly present. Yes, MS does have a coolant temp advance/retard feature. I'll check it out to see if I can turn it off or at least make it work for me instead of against me. I remain frustrated why I am getting selective changes to only one of the cylinders on each coil bank. I have not touched any of the earths which are all inside the car in the dry since I built it. The same earth point is used for my fuel pump, ECU and all sensors. But I will check nonetheless Ron. Weren't your problems to do with shielding the VR cable Ron ? Ta. Richard. Minivanless, but reluctantly happy living with the decision. There'll be another one day.
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![]() 11046 Posts Member #: 965 Post Whore Preston On The Brook |
30th Jan, 2011 at 11:41:37pm
Is the crank sensor close enough to the trigger and does the trigger have any run out?
On 26th Oct, 2004 TurboDave16v said:
Is it A-Series only? I think it should be... So when some joey comes on here about how his 16v turbo vauxhall is great compared to ours, he can be given the 'bird'... On 26th Oct, 2004 Tom Fenton said:
Yep I agree with TD........ |
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![]() 1105 Posts Member #: 1504 Post Whore Westbury, Wiltshire |
31st Jan, 2011 at 12:32:58am
Rod/Sprocket.
Minivanless, but reluctantly happy living with the decision. There'll be another one day.
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5988 Posts Member #: 2024 Formally Retired Rural Suffolk |
31st Jan, 2011 at 08:49:10am
The settings are quoted slightly differently in MS2, ie, we don't have to set trigger and trigger return - but as the A and B are 18 apart, that shouldn't be the problem.
Schrödinger's cat - so which one am I ??? |
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![]() 1105 Posts Member #: 1504 Post Whore Westbury, Wiltshire |
31st Jan, 2011 at 11:23:56am
Thanks Rod.
Minivanless, but reluctantly happy living with the decision. There'll be another one day.
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![]() 10023 Posts Member #: 1456 Mongo Barnsley, South Flatcapshire |
31st Jan, 2011 at 11:27:18am
Could you try your old dizzy? This would eliminate MS issues and tell you if your mixture etc is wrong. If something is worth doing, it's worth doing half of. |
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3006 Posts Member #: 2500 Post Whore Buckinghamshire |
31st Jan, 2011 at 01:37:34pm
Do try to keep up John, Richard told us earlier that he had sold the dizzy ! |
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![]() 10023 Posts Member #: 1456 Mongo Barnsley, South Flatcapshire |
31st Jan, 2011 at 01:38:52pm
Me no ready very good sometimes. If something is worth doing, it's worth doing half of. |
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3006 Posts Member #: 2500 Post Whore Buckinghamshire |
31st Jan, 2011 at 01:41:55pm
Maybe so, but you must read bloody quick to have got back so fast !! |
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![]() 6753 Posts Member #: 828 Post Whore uranus |
31st Jan, 2011 at 06:27:33pm
richard , although you say that a leak on the inlet to 1/2 would not make it rich ,a leak on 3/4 would make it rich on 1/2 if you adjusted the carb to be right for 3/4 .maybe thats why you have the screw in so far ? Medusa + injection = too much torque for the dyno ..https://youtu.be/qg5o0_tJxYM |
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![]() 1105 Posts Member #: 1504 Post Whore Westbury, Wiltshire |
31st Jan, 2011 at 06:38:08pm
On 31st Jan, 2011 robert said:
richard , although you say that a leak on the inlet to 1/2 would not make it rich ,a leak on 3/4 would make it rich on 1/2 if you adjusted the carb to be right for 3/4 .maybe thats why you have the screw in so far ? Yeah Robert, that's what I'm thinking too. But why is the spark rate for 1 and 2 slower and with noticeable gaps on the strobe, than 3 and 4 ? 1 is slower than 4 but they're from the same coil and 2 is slower than 3 but they too are from the same coil. Surely none of that should happen even if there was an air leak present on the inlet tract to 3/4 ? I'm gonna do the dwell and HT coilpack earth checks when I get back Tuesday evening. Cheers. Richard. Minivanless, but reluctantly happy living with the decision. There'll be another one day.
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![]() 6753 Posts Member #: 828 Post Whore uranus |
31st Jan, 2011 at 09:13:04pm
possibly the spark is running down the insulator which is wet from the rich mix ? so the kv doesnt build up to a high enough level to trigger the strobe ? Medusa + injection = too much torque for the dyno ..https://youtu.be/qg5o0_tJxYM |
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![]() 1105 Posts Member #: 1504 Post Whore Westbury, Wiltshire |
1st Feb, 2011 at 01:21:14pm
On 31st Jan, 2011 robert said:
possibly the spark is running down the insulator which is wet from the rich mix ? so the kv doesnt build up to a high enough level to trigger the strobe ? I like that explanation, makes sense. No 2 plug in particular is very very wet with unburnt fuel when you pop it out after a 30 second run from cold. Might have to postpone working on the van tonight as the immersion tank in the cottage has just sprung a leak and I need to go plumbing tonight to fix the bugger ! Richard. Minivanless, but reluctantly happy living with the decision. There'll be another one day.
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![]() 1105 Posts Member #: 1504 Post Whore Westbury, Wiltshire |
1st Feb, 2011 at 10:05:14pm
Right guys.
Minivanless, but reluctantly happy living with the decision. There'll be another one day.
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![]() 2406 Posts Member #: 341 aka T2clubby South Staffs |
1st Feb, 2011 at 10:40:26pm
Try spraying some carb cleaner around the manifold face to prove a leak in the gasket. My money is on fueling rather than ignition mate.
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![]() 558 Posts Member #: 8143 Post Whore London |
1st Feb, 2011 at 11:29:58pm
I reckon its fueling/air leak too.
Edited by dischub on 1st Feb, 2011. |
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